> 4 Items:
> 1: What was the printer and toner that worked and didn't?
> 2: For a drill press, I have used Dremel with very good results. I also
> have a 16.5" Delta drill press with 1/16" - 5/8" chuck, and then a
> smaller drill size chuck that can be gripped, but wouldn't even think of
> using that, although the small drill bits with 1/8" shanks can be
> gripped easily. Get the regular PCB drills with 1/8" shanks and short
> drill spiral lengths. The long drill bits with same shank diameter as
> drill size get slight bends, wobble, and eventually break.
> 3: When making the PCB print image, every hole should have a small size
> hole etched in the copper. This becomes the equivalent of an accurately
> located center punch to get the drill started at the right location. The
> drill will wander to that depression if you get close to the location.
> 4: For double sided boards, I include a donut at 4 corners, both sides.
> Pin prick through the paper before ironing on the first side, drill the
> 4 holes through the board, use pins through the papers and holes to
> align, and iron on the 2nd side. Have had good results with careful
> work, but there are limits to the accuracy. Dips with 0.1" spacing
> should be no problem if there are not traces between the pads. With
> traces between, probably will scrap some boards, probably would solder
> wire across for the a few to be made. :)
>
>
> solarwind wrote:
>
>> I etched my first PCB today. It came out very well (considering that
>> it was the first one I did). I used a mix of different techniques
>> which all worked out well for me in the end.
>>
>> To begin, I made a simple design for a quick prototype board for my
>> dsPIC33FJ128GP802. The board itself is very small, just about 1.5" x
>> 2.5" (off the top of my head). I had a large sheet of copper clad
>> board so I had to cut out the small piece that I would be working
>> with. This part was not fun at all.
>>
>> I printed out my design and traced out the rectangle off a corner of
>> the large copper clad board. I then used a utility knife to score the
>> sides of my design. It took a while to get deep enough to snap. Then I
>> used metal shears to cut one edge of the board. This was an unclean
>> cut and damaged part of the large board and slightly warped the copper
>> on my design. No big deal. I then stuck the remaining part of the
>> board into a vice (with paper towel for padding) and snapped the
>> remaining edge. I then sanded the sides with a piece of (metal
>> purpose) sand paper. I was then left with a small rectangle of copper
>> board ready to be used for toner transfer. I used nail polish remover
>> to clean the board. Then I used soap and continued to clean the board.
>> Finally, I took some fine sandpaper and scrubbed the board clean. The
>> board was now ready for toner transfer.
>>
>> >From suggestions from my other thread, I tried a different printer. I
>> used the same paper (staples glossy paper for laser printers) that I
>> had tried before. I set the print quality to the highest setting and
>> configured it to deposit the most amount of toner possible. I then cut
>> out my design and headed over to my clothes iron. I preheated the
>> board by placing a blank sheet of paper of my board and ironing it for
>> about a minute. Then I carefully placed my design onto the copper
>> board. It stuck instantly. I ironed it for about 2 minutes. (60 of
>> those seconds I just left the iron on top and went downstairs to get a
>> snack). I didn't do anything special. I just pressed hard (but not too
>> hard) and went over it with the tip of the iron. I then filled a small
>> sandwich box with water (about body temperature) and dropped my board
>> (with the design paper still stuck on it) into the water. I headed
>> over to my local grocery store to get some groceries for dinner. By
>> the time I came back, the paper was soft enough to peel and rub off
>> with my thumb. Some of the toner smudged, but overall, the quality was
>> pretty good. The toner had definitely stuck well this time.
>>
>> Now for the etching part. I took a small dish washing sponge and cut
>> out a square about 3" x 3" x 0.75". I poured about a table spoon of
>> ferric chloride on the sponge. I put on my vinyl gloves and started
>> lightly wiping the board with the sponge. The copper started to come
>> off instantly and turned the bright-yellow sponge nearly black. I kept
>> wiping for about 2 - 4 minutes and eventually, all of the copper (that
>> was not protected by the toner, of course) came off. This sponge
>> method turned out to be very fast, efficient, clean and easy. Also
>> saved a lot of ferric chloride. I ended up with a very well etched
>> board. It was easy to see when it was finished and the etching
>> solution worked very fast and etched very cleanly. Then I washed the
>> board and inspected it (and admired it). It would have been perfect
>> had the toner not smudged. The etching process itself was very clean
>> and precise. The only trouble was the toner. I need to find a better
>> way to put etchant-resist onto my copper.
>>
>> I then took the almost-finished board downstairs to drill. This part
>> was not fun as well. I drilled about two holes then gave up because
>> all I had was a clunky drill and very brittle drill bits. This
>> drilling part is impossible without a proper drill press. A CNC
>> machine would be ideal (even a crude one would do the job
>> sufficiently). So there ya have it. An almost-finished PCB.
>>
>> Looks like I'll need to find myself a drill press.
>>
>> To all the helped and gave advice, thank you very much. This process
>> turned out to be fun and educational and I leaned a skill that I'm
>> sure I'll find very useful in the future. The whole process took less
>> than an hour and gave very good results. The results would have been
>> perfect if I had a better method to transfer the toner (via laminator
>> and a good printer, maybe) and a CNC machine or at least a drill
>> press.
>>
>> What I was most impressed with was the sponge method of etching. Only
>> a table spoon of ferric chloride was required and none of that
>> heating/agitation nonsense was needed. The process was clean and
>> efficient - no spills, little to clean up afterward. So if there's any
>> of you still pouring the etching solution into a tub and
>> heating/agitating, I highly recommend that you give the sponge method
>> a try. It's awesome!
>>
>> -- [ solarwind ] --
http://solar-blogg.blogspot.com/
>>
>>